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Loose exhaust manifold, part 4 |
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Plan- |
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Unfortunately, my old head did not have enough thickness for
another milling. This meant buying another head. I
thought about having some extra work done while this head was in a
shop, but it wasn't in the budget. It wasn't until my
rod knock that I was
able to build the head. |
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Project- |
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It took 5 days for the machine shop to get another head in and build
it up.
I only did one thing besides remove the plastic and the wood strips
along the bottom, and that was install the new cam seals.
I used a large socket as the install tool, and just gently tapped it
in with a hammer. |
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The 34 hours of work that I have totaled here is the amount of time
the shop spent taking the old parts out of the old head and putting them
into the new one. Since the head is brand new, I decided not
to have the heli-coils installed. |
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After two blown head gaskets, I think I need to take active measures to
ensure I don't warp this new head. There has been some discussion
about how the back part of the engine bay is so much hotter than the
front, I think I will vent
the hood somehow. |
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While I was waiting for the head, I
detailed the
engine bay. |
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Difficulty- |
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1- Be careful when moving the head around- with the cams installed the
valves stick out the bottom and are vulnerable. My new head came
with 2 wood strips so the head could be set down without the vavles
touching. |
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Problems- |
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None |
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Intermission- |
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It sure is all pretty, nice, and clean. Time to
install it. |
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Brand new head |
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Another view |
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Last updated:
Freitag Oktober 21, 2005
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Time |
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144 hours (34 hours here) |
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Total costs |
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$1,683.50 ($637.00 here) |
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Materials &
parts |
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New head- $637.00 |
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Tools |
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Knife |
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Hammer |
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Large socket |
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